Message ID | E1dwsgD-0006Hy-5u@rmk-PC.armlinux.org.uk (mailing list archive) |
---|---|
State | Accepted |
Headers | show |
On Tue, Sep 26, 2017 at 05:25:53PM +0100, Russell King wrote: > A 2us delay is too small for the bus to settle after writing to the > register. Extend to 10us which gives more reliable results. > > Signed-off-by: Russell King <rmk+kernel@armlinux.org.uk> Applied, thank you. > --- > drivers/input/serio/sa1111ps2.c | 2 +- > 1 file changed, 1 insertion(+), 1 deletion(-) > > diff --git a/drivers/input/serio/sa1111ps2.c b/drivers/input/serio/sa1111ps2.c > index f1c036260d25..f9e5c793f4f0 100644 > --- a/drivers/input/serio/sa1111ps2.c > +++ b/drivers/input/serio/sa1111ps2.c > @@ -212,7 +212,7 @@ static unsigned int ps2_test_one(struct ps2if *ps2if, > > writel_relaxed(PS2CR_ENA | mask, ps2if->base + PS2CR); > > - udelay(2); > + udelay(10); > > val = readl_relaxed(ps2if->base + PS2STAT); > return val & (PS2STAT_KBC | PS2STAT_KBD); > -- > 2.7.4 >
diff --git a/drivers/input/serio/sa1111ps2.c b/drivers/input/serio/sa1111ps2.c index f1c036260d25..f9e5c793f4f0 100644 --- a/drivers/input/serio/sa1111ps2.c +++ b/drivers/input/serio/sa1111ps2.c @@ -212,7 +212,7 @@ static unsigned int ps2_test_one(struct ps2if *ps2if, writel_relaxed(PS2CR_ENA | mask, ps2if->base + PS2CR); - udelay(2); + udelay(10); val = readl_relaxed(ps2if->base + PS2STAT); return val & (PS2STAT_KBC | PS2STAT_KBD);
A 2us delay is too small for the bus to settle after writing to the register. Extend to 10us which gives more reliable results. Signed-off-by: Russell King <rmk+kernel@armlinux.org.uk> --- drivers/input/serio/sa1111ps2.c | 2 +- 1 file changed, 1 insertion(+), 1 deletion(-)