From patchwork Wed Jul 8 21:14:21 2020 Content-Type: text/plain; charset="utf-8" MIME-Version: 1.0 Content-Transfer-Encoding: 7bit X-Patchwork-Submitter: Hans de Goede X-Patchwork-Id: 11652563 Return-Path: Received: from mail.kernel.org (pdx-korg-mail-1.web.codeaurora.org [172.30.200.123]) by pdx-korg-patchwork-2.web.codeaurora.org (Postfix) with ESMTP id 7701160D for ; Wed, 8 Jul 2020 21:15:04 +0000 (UTC) Received: from gabe.freedesktop.org (gabe.freedesktop.org [131.252.210.177]) (using TLSv1.2 with cipher ECDHE-RSA-AES256-GCM-SHA384 (256/256 bits)) (No client certificate requested) by mail.kernel.org (Postfix) with ESMTPS id 56E1E206E9 for ; Wed, 8 Jul 2020 21:15:04 +0000 (UTC) Authentication-Results: mail.kernel.org; dkim=fail reason="signature verification failed" (1024-bit key) header.d=redhat.com header.i=@redhat.com header.b="ONhDF7OI" DMARC-Filter: OpenDMARC Filter v1.3.2 mail.kernel.org 56E1E206E9 Authentication-Results: mail.kernel.org; dmarc=fail (p=none dis=none) header.from=redhat.com Authentication-Results: mail.kernel.org; spf=none smtp.mailfrom=dri-devel-bounces@lists.freedesktop.org Received: from gabe.freedesktop.org (localhost [127.0.0.1]) by gabe.freedesktop.org (Postfix) with ESMTP id 461FB6E446; Wed, 8 Jul 2020 21:14:56 +0000 (UTC) X-Original-To: dri-devel@lists.freedesktop.org Delivered-To: dri-devel@lists.freedesktop.org Received: from us-smtp-delivery-1.mimecast.com (us-smtp-2.mimecast.com [207.211.31.81]) by gabe.freedesktop.org (Postfix) with ESMTPS id 98A5E6E446 for ; Wed, 8 Jul 2020 21:14:55 +0000 (UTC) DKIM-Signature: v=1; a=rsa-sha256; c=relaxed/relaxed; d=redhat.com; s=mimecast20190719; t=1594242894; h=from:from:reply-to:subject:subject:date:date:message-id:message-id: to:to:cc:cc:mime-version:mime-version: content-transfer-encoding:content-transfer-encoding: in-reply-to:in-reply-to:references:references; bh=aMEAQ1K28IcwheGcPcbAGTXILoPdfisVvobXNqzUOek=; b=ONhDF7OI/96ZNR+M2IN7WXafWViqmwHcI99k6m29sWOgexZupCyMshNWCQ7xVSPIOPMsw0 KJ8apUhzj58jf3SjG70NwXAiyGWJ/sW3AtXy9O0+zsGNiwCup0T12pu25v/qsrxlYY1sBU FIAZXRHTxBP7l6DhrgoyeNkAGwEp/UA= Received: from mimecast-mx01.redhat.com (mimecast-mx01.redhat.com [209.132.183.4]) (Using TLS) by relay.mimecast.com with ESMTP id us-mta-435-XOqSayTYNjKfHSSTic1ZLw-1; Wed, 08 Jul 2020 17:14:52 -0400 X-MC-Unique: XOqSayTYNjKfHSSTic1ZLw-1 Received: from smtp.corp.redhat.com (int-mx03.intmail.prod.int.phx2.redhat.com [10.5.11.13]) (using TLSv1.2 with cipher AECDH-AES256-SHA (256/256 bits)) (No client certificate requested) by mimecast-mx01.redhat.com (Postfix) with ESMTPS id D639BE919; Wed, 8 Jul 2020 21:14:50 +0000 (UTC) Received: from x1.localdomain.com (ovpn-112-5.ams2.redhat.com [10.36.112.5]) by smtp.corp.redhat.com (Postfix) with ESMTP id 4FEA279220; Wed, 8 Jul 2020 21:14:48 +0000 (UTC) From: Hans de Goede To: Thierry Reding , =?utf-8?q?Uwe_Kleine-K=C3=B6n?= =?utf-8?q?ig?= , Jani Nikula , Joonas Lahtinen , Rodrigo Vivi , =?utf-8?b?VmlsbGUgU3lyasOkbMOk?= , "Rafael J . Wysocki" , Len Brown Subject: [PATCH v4 05/16] pwm: lpss: Use pwm_lpss_apply() when restoring state on resume Date: Wed, 8 Jul 2020 23:14:21 +0200 Message-Id: <20200708211432.28612-6-hdegoede@redhat.com> In-Reply-To: <20200708211432.28612-1-hdegoede@redhat.com> References: <20200708211432.28612-1-hdegoede@redhat.com> MIME-Version: 1.0 X-Scanned-By: MIMEDefang 2.79 on 10.5.11.13 X-BeenThere: dri-devel@lists.freedesktop.org X-Mailman-Version: 2.1.29 Precedence: list List-Id: Direct Rendering Infrastructure - Development List-Unsubscribe: , List-Archive: List-Post: List-Help: List-Subscribe: , Cc: linux-pwm@vger.kernel.org, linux-acpi@vger.kernel.org, intel-gfx , dri-devel@lists.freedesktop.org, Hans de Goede , Andy Shevchenko , Mika Westerberg Errors-To: dri-devel-bounces@lists.freedesktop.org Sender: "dri-devel" Before this commit a suspend + resume of the LPSS PWM controller would result in the controller being reset to its defaults of output-freq = clock/256, duty-cycle=100%, until someone changes to the output-freq and/or duty-cycle are made. This problem has been masked so far because the main consumer (the i915 driver) was always making duty-cycle changes on resume. With the conversion of the i915 driver to the atomic PWM API the driver now only disables/enables the PWM on suspend/resume leaving the output-freq and duty as is, triggering this problem. The LPSS PWM controller has a mechanism where the ctrl register value and the actual base-unit and on-time-div values used are latched. When software sets the SW_UPDATE bit then at the end of the current PWM cycle, the new values from the ctrl-register will be latched into the actual registers, and the SW_UPDATE bit will be cleared. The problem is that before this commit our suspend/resume handling consisted of simply saving the PWM ctrl register on suspend and restoring it on resume, without setting the PWM_SW_UPDATE bit. When the controller has lost its state over a suspend/resume and thus has been reset to the defaults, just restoring the register is not enough. We must also set the SW_UPDATE bit to tell the controller to latch the restored values into the actual registers. Fixing this problem is not as simple as just or-ing in the value which is being restored with SW_UPDATE. If the PWM was enabled before we must write the new settings + PWM_SW_UPDATE before setting PWM_ENABLE. We must also wait for PWM_SW_UPDATE to become 0 again and depending on the model we must do this either before or after the setting of PWM_ENABLE. All the necessary logic for doing this is already present inside pwm_lpss_apply(), so instead of duplicating this inside the resume handler, this commit makes the resume handler use pwm_lpss_apply() to restore the settings when necessary. This fixes the output-freq and duty-cycle being reset to their defaults on resume. Signed-off-by: Hans de Goede --- Changes in v3: - This replaces the "pwm: lpss: Set SW_UPDATE bit when enabling the PWM" patch from previous versions of this patch-set, which really was a hack working around the resume issue which this patch fixes properly. --- drivers/pwm/pwm-lpss.c | 62 ++++++++++++++++++++++++++++++++++++------ 1 file changed, 53 insertions(+), 9 deletions(-) diff --git a/drivers/pwm/pwm-lpss.c b/drivers/pwm/pwm-lpss.c index 80d0f9c64f9d..4f3d60ce9929 100644 --- a/drivers/pwm/pwm-lpss.c +++ b/drivers/pwm/pwm-lpss.c @@ -123,25 +123,31 @@ static inline void pwm_lpss_cond_enable(struct pwm_device *pwm, bool cond) pwm_lpss_write(pwm, pwm_lpss_read(pwm) | PWM_ENABLE); } -static int pwm_lpss_apply(struct pwm_chip *chip, struct pwm_device *pwm, - const struct pwm_state *state) +static int __pwm_lpss_apply(struct pwm_chip *chip, struct pwm_device *pwm, + const struct pwm_state *state, bool from_resume) { struct pwm_lpss_chip *lpwm = to_lpwm(chip); int ret; if (state->enabled) { if (!pwm_is_enabled(pwm)) { - pm_runtime_get_sync(chip->dev); + if (!from_resume) + pm_runtime_get_sync(chip->dev); + ret = pwm_lpss_is_updating(pwm); if (ret) { - pm_runtime_put(chip->dev); + if (!from_resume) + pm_runtime_put(chip->dev); + return ret; } pwm_lpss_prepare(lpwm, pwm, state->duty_cycle, state->period); pwm_lpss_cond_enable(pwm, lpwm->info->bypass == false); ret = pwm_lpss_wait_for_update(pwm); if (ret) { - pm_runtime_put(chip->dev); + if (!from_resume) + pm_runtime_put(chip->dev); + return ret; } pwm_lpss_cond_enable(pwm, lpwm->info->bypass == true); @@ -154,12 +160,20 @@ static int pwm_lpss_apply(struct pwm_chip *chip, struct pwm_device *pwm, } } else if (pwm_is_enabled(pwm)) { pwm_lpss_write(pwm, pwm_lpss_read(pwm) & ~PWM_ENABLE); - pm_runtime_put(chip->dev); + + if (!from_resume) + pm_runtime_put(chip->dev); } return 0; } +static int pwm_lpss_apply(struct pwm_chip *chip, struct pwm_device *pwm, + const struct pwm_state *state) +{ + return __pwm_lpss_apply(chip, pwm, state, false); +} + static void pwm_lpss_get_state(struct pwm_chip *chip, struct pwm_device *pwm, struct pwm_state *state) { @@ -272,10 +286,40 @@ EXPORT_SYMBOL_GPL(pwm_lpss_suspend); int pwm_lpss_resume(struct device *dev) { struct pwm_lpss_chip *lpwm = dev_get_drvdata(dev); - int i; + struct pwm_state saved_state; + struct pwm_device *pwm; + int i, ret; + u32 ctrl; - for (i = 0; i < lpwm->info->npwm; i++) - writel(lpwm->saved_ctrl[i], lpwm->regs + i * PWM_SIZE + PWM); + for (i = 0; i < lpwm->info->npwm; i++) { + pwm = &lpwm->chip.pwms[i]; + + ctrl = pwm_lpss_read(pwm); + /* If we did not reach S0i3/S3 the controller keeps its state */ + if (ctrl == lpwm->saved_ctrl[i]) + continue; + + /* + * We cannot just blindly restore the old value here. Since we + * are changing the settings we must set SW_UPDATE and if the + * PWM was enabled before we must write the new settings + + * PWM_SW_UPDATE before setting PWM_ENABLE. We must also wait + * for PWM_SW_UPDATE to become 0 again and depending on the + * model we must do this either before or after the setting of + * PWM_ENABLE. + * So instead of reproducing all the code from pwm_apply() here, + * we just reapply the state as stored in pwm->state. + */ + saved_state = pwm->state; + /* + * Update enabled to its actual setting for the + * enabled<->disabled transitions inside apply(). + */ + pwm->state.enabled = !!(ctrl & PWM_ENABLE); + ret = __pwm_lpss_apply(&lpwm->chip, pwm, &saved_state, true); + if (ret) + dev_err(dev, "Error restoring state on resume\n"); + } return 0; }