Message ID | 20231010153812.2869633-2-amadeus@jmu.edu.cn (mailing list archive) |
---|---|
State | New, archived |
Headers | show |
Series | [1/2] arm64: dts: allwinner: h616: move emac delay back to Orange Pi Zero 2 DT | expand |
Hi! Dne torek, 10. oktober 2023 ob 17:38:12 CEST je Chukun Pan napisal(a): > Add the correct delay value to emac. Also add missing mdio > properties for the YT8531 PHY (clock output required). > With these changes, Ethernet now looks stable. This is also a fix, so it would also deserve Fixes tag. In fact, please merge previous and this patch into one. After all, you are fixing only one thing - ethernet on OrangePi Zero 3 board. Can you also explain how did you figure out that additional PHY properties are needed? At first glance, based on description of motorcomm,keep-pll-enabled, it's not immediately clear why it should be needed. Same goes for second property. 1800 ps delay basically means that rgmii is not correct type and rgmii-rxid should be used instead. Indeed, schematic confirms that's the case. With that, allwinner,rx-delay-ps can be 0 and thus ommited from DT file. Since there is many differences, I suggest that you remove whole emac0 node from common DTSI file and put specific ones to each board. It will be less confusing that way. Best regards, Jernej > > Signed-off-by: Chukun Pan <amadeus@jmu.edu.cn> > --- > arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts | 4 ++++ > 1 file changed, 4 insertions(+) > > diff --git a/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts b/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts > index 00fe28caac93..02c7836b624a 100644 > --- a/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts > +++ b/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts > @@ -13,10 +13,14 @@ / { > }; > > &emac0 { > + allwinner,rx-delay-ps = <1800>; > + allwinner,tx-delay-ps = <700>; > phy-supply = <®_dldo1>; > }; > > &ext_rgmii_phy { > + motorcomm,keep-pll-enabled; > + motorcomm,auto-sleep-disabled; > motorcomm,clk-out-frequency-hz = <125000000>; > }; > >
> Can you also explain how did you figure out that additional PHY properties > are needed? At first glance, based on description of motorcomm,keep-pll-enabled, > it's not immediately clear why it should be needed. Same goes for second > property. This is based on a search for 'motorcomm,clk-out-frequency-hz = <125000000>' in the kernel. Refer to device tree of other devices with the same properties. After a simple short test, it seems that it is unnecessary. I will delete these two properties in patch v2. > 1800 ps delay basically means that rgmii is not correct type and rgmii-rxid > should be used instead. Indeed, schematic confirms that's the case. With that, > allwinner,rx-delay-ps can be 0 and thus ommited from DT file. Thanks, rgmii-rxid works for me. Will be corrected in patch v2. Thanks, Chukun
diff --git a/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts b/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts index 00fe28caac93..02c7836b624a 100644 --- a/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts +++ b/arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts @@ -13,10 +13,14 @@ / { }; &emac0 { + allwinner,rx-delay-ps = <1800>; + allwinner,tx-delay-ps = <700>; phy-supply = <®_dldo1>; }; &ext_rgmii_phy { + motorcomm,keep-pll-enabled; + motorcomm,auto-sleep-disabled; motorcomm,clk-out-frequency-hz = <125000000>; };
Add the correct delay value to emac. Also add missing mdio properties for the YT8531 PHY (clock output required). With these changes, Ethernet now looks stable. Signed-off-by: Chukun Pan <amadeus@jmu.edu.cn> --- arch/arm64/boot/dts/allwinner/sun50i-h618-orangepi-zero3.dts | 4 ++++ 1 file changed, 4 insertions(+)