diff mbox

[V2] hwrng: OMAP: Fix assumption that runtime_get_sync will always succeed

Message ID 1466787040-26184-1-git-send-email-nm@ti.com (mailing list archive)
State New, archived
Headers show

Commit Message

Nishanth Menon June 24, 2016, 4:50 p.m. UTC
pm_runtime_get_sync does return a error value that must be checked for
error conditions, else, due to various reasons, the device maynot be
enabled and the system will crash due to lack of clock to the hardware
module.

Before:
12.562784] [00000000] *pgd=fe193835
12.562792] Internal error: : 1406 [#1] SMP ARM
[...]
12.562864] CPU: 1 PID: 241 Comm: modprobe Not tainted 4.7.0-rc4-next-20160624 #2
12.562867] Hardware name: Generic DRA74X (Flattened Device Tree)
12.562872] task: ed51f140 ti: ed44c000 task.ti: ed44c000
12.562886] PC is at omap4_rng_init+0x20/0x84 [omap_rng]
12.562899] LR is at set_current_rng+0xc0/0x154 [rng_core]
[...]

After the proper checks:
[   94.366705] omap_rng 48090000.rng: _od_fail_runtime_resume: FIXME:
missing hwmod/omap_dev info
[   94.375767] omap_rng 48090000.rng: Failed to runtime_get device -19
[   94.382351] omap_rng 48090000.rng: initialization failed.

Fixes: 665d92fa85b5 ("hwrng: OMAP: convert to use runtime PM")
Cc: Paul Walmsley <paul@pwsan.com>
Signed-off-by: Nishanth Menon <nm@ti.com>
---
Changes in V2:
	- Added runtime_put_noidle when get_sync fails to ensure proper refcounting

V1: https://patchwork.kernel.org/patch/9197855/

Patch based on: next-20160624
Issue seen with next-20160624
Full crash log: http://pastebin.ubuntu.com/17801376/

 drivers/char/hw_random/omap-rng.c | 16 ++++++++++++++--
 1 file changed, 14 insertions(+), 2 deletions(-)

Comments

Herbert Xu June 27, 2016, 9:05 a.m. UTC | #1
On Fri, Jun 24, 2016 at 11:50:39AM -0500, Nishanth Menon wrote:
> pm_runtime_get_sync does return a error value that must be checked for
> error conditions, else, due to various reasons, the device maynot be
> enabled and the system will crash due to lack of clock to the hardware
> module.
> 
> Before:
> 12.562784] [00000000] *pgd=fe193835
> 12.562792] Internal error: : 1406 [#1] SMP ARM
> [...]
> 12.562864] CPU: 1 PID: 241 Comm: modprobe Not tainted 4.7.0-rc4-next-20160624 #2
> 12.562867] Hardware name: Generic DRA74X (Flattened Device Tree)
> 12.562872] task: ed51f140 ti: ed44c000 task.ti: ed44c000
> 12.562886] PC is at omap4_rng_init+0x20/0x84 [omap_rng]
> 12.562899] LR is at set_current_rng+0xc0/0x154 [rng_core]
> [...]
> 
> After the proper checks:
> [   94.366705] omap_rng 48090000.rng: _od_fail_runtime_resume: FIXME:
> missing hwmod/omap_dev info
> [   94.375767] omap_rng 48090000.rng: Failed to runtime_get device -19
> [   94.382351] omap_rng 48090000.rng: initialization failed.
> 
> Fixes: 665d92fa85b5 ("hwrng: OMAP: convert to use runtime PM")
> Cc: Paul Walmsley <paul@pwsan.com>
> Signed-off-by: Nishanth Menon <nm@ti.com>
> ---
> Changes in V2:
> 	- Added runtime_put_noidle when get_sync fails to ensure proper refcounting

Patch applied.  Thanks.
diff mbox

Patch

diff --git a/drivers/char/hw_random/omap-rng.c b/drivers/char/hw_random/omap-rng.c
index 8a1432e8bb80..01d4be2c354b 100644
--- a/drivers/char/hw_random/omap-rng.c
+++ b/drivers/char/hw_random/omap-rng.c
@@ -384,7 +384,12 @@  static int omap_rng_probe(struct platform_device *pdev)
 	}
 
 	pm_runtime_enable(&pdev->dev);
-	pm_runtime_get_sync(&pdev->dev);
+	ret = pm_runtime_get_sync(&pdev->dev);
+	if (ret) {
+		dev_err(&pdev->dev, "Failed to runtime_get device: %d\n", ret);
+		pm_runtime_put_noidle(&pdev->dev);
+		goto err_ioremap;
+	}
 
 	ret = (dev->of_node) ? of_get_omap_rng_device_details(priv, pdev) :
 				get_omap_rng_device_details(priv);
@@ -435,8 +440,15 @@  static int __maybe_unused omap_rng_suspend(struct device *dev)
 static int __maybe_unused omap_rng_resume(struct device *dev)
 {
 	struct omap_rng_dev *priv = dev_get_drvdata(dev);
+	int ret;
+
+	ret = pm_runtime_get_sync(dev);
+	if (ret) {
+		dev_err(dev, "Failed to runtime_get device: %d\n", ret);
+		pm_runtime_put_noidle(dev);
+		return ret;
+	}
 
-	pm_runtime_get_sync(dev);
 	priv->pdata->init(priv);
 
 	return 0;