diff mbox

[09/35] arm64: dts: m3ulcb: Fix EthernetAVB PHY timing

Message ID bdb3656e4c085de6f44b162554c2793492577834.1495457812.git.horms+renesas@verge.net.au (mailing list archive)
State Accepted
Commit bdb3656e4c085de6f44b162554c2793492577834
Delegated to: Simon Horman
Headers show

Commit Message

Simon Horman May 22, 2017, 1:58 p.m. UTC
Set PHY rxc-skew-ps to 1500 and all other values to their default values.

This is intended to to address failures in the case of 1Gbps communication
using the salvator-x board with the KSZ9031RNX phy. This has been
reported to occur with both the r8a7795 (H3) and r8a7796 (M3-W) SoCs.

Based in a similar patch for the r8a7796 salvator-x by Kazuya Mizuguchi.

Signed-off-by: Simon Horman <horms+renesas@verge.net.au>
---
 arch/arm64/boot/dts/renesas/r8a7796-m3ulcb.dts | 13 +------------
 1 file changed, 1 insertion(+), 12 deletions(-)
diff mbox

Patch

diff --git a/arch/arm64/boot/dts/renesas/r8a7796-m3ulcb.dts b/arch/arm64/boot/dts/renesas/r8a7796-m3ulcb.dts
index c2a4549d3738..440d93e8388d 100644
--- a/arch/arm64/boot/dts/renesas/r8a7796-m3ulcb.dts
+++ b/arch/arm64/boot/dts/renesas/r8a7796-m3ulcb.dts
@@ -169,18 +169,7 @@ 
 	status = "okay";
 
 	phy0: ethernet-phy@0 {
-		rxc-skew-ps = <900>;
-		rxdv-skew-ps = <0>;
-		rxd0-skew-ps = <0>;
-		rxd1-skew-ps = <0>;
-		rxd2-skew-ps = <0>;
-		rxd3-skew-ps = <0>;
-		txc-skew-ps = <900>;
-		txen-skew-ps = <0>;
-		txd0-skew-ps = <0>;
-		txd1-skew-ps = <0>;
-		txd2-skew-ps = <0>;
-		txd3-skew-ps = <0>;
+		rxc-skew-ps = <1500>;
 		reg = <0>;
 		interrupt-parent = <&gpio2>;
 		interrupts = <11 IRQ_TYPE_LEVEL_LOW>;