diff mbox series

[4.9] can: bcm: fix UAF of bcm op

Message ID 20220128064054.2434068-1-william.xuanziyang@huawei.com (mailing list archive)
State Awaiting Upstream
Delegated to: Netdev Maintainers
Headers show
Series [4.9] can: bcm: fix UAF of bcm op | expand

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Context Check Description
netdev/tree_selection success Series ignored based on subject

Commit Message

Ziyang Xuan (William) Jan. 28, 2022, 6:40 a.m. UTC
Stopping tasklet and hrtimer rely on the active state of tasklet and
hrtimer sequentially in bcm_remove_op(), the op object will be freed
if they are all unactive. Assume the hrtimer timeout is short, the
hrtimer cb has been excuted after tasklet conditional judgment which
must be false after last round tasklet_kill() and before condition
hrtimer_active(), it is false when execute to hrtimer_active(). Bug
is triggerd, because the stopping action is end and the op object
will be freed, but the tasklet is scheduled. The resources of the op
object will occur UAF bug.

Move hrtimer_cancel() behind tasklet_kill() and switch 'while () {...}'
to 'do {...} while ()' to fix the op UAF problem.

Fixes: a06393ed0316 ("can: bcm: fix hrtimer/tasklet termination in bcm op removal")
Reported-by: syzbot+5ca851459ed04c778d1d@syzkaller.appspotmail.com
Cc: stable@vger.kernel.org
Signed-off-by: Ziyang Xuan <william.xuanziyang@huawei.com>
---
 net/can/bcm.c | 20 ++++++++++----------
 1 file changed, 10 insertions(+), 10 deletions(-)

Comments

Greg Kroah-Hartman Jan. 29, 2022, 11:41 a.m. UTC | #1
On Fri, Jan 28, 2022 at 02:40:54PM +0800, Ziyang Xuan wrote:
> Stopping tasklet and hrtimer rely on the active state of tasklet and
> hrtimer sequentially in bcm_remove_op(), the op object will be freed
> if they are all unactive. Assume the hrtimer timeout is short, the
> hrtimer cb has been excuted after tasklet conditional judgment which
> must be false after last round tasklet_kill() and before condition
> hrtimer_active(), it is false when execute to hrtimer_active(). Bug
> is triggerd, because the stopping action is end and the op object
> will be freed, but the tasklet is scheduled. The resources of the op
> object will occur UAF bug.
> 
> Move hrtimer_cancel() behind tasklet_kill() and switch 'while () {...}'
> to 'do {...} while ()' to fix the op UAF problem.
> 
> Fixes: a06393ed0316 ("can: bcm: fix hrtimer/tasklet termination in bcm op removal")
> Reported-by: syzbot+5ca851459ed04c778d1d@syzkaller.appspotmail.com
> Cc: stable@vger.kernel.org
> Signed-off-by: Ziyang Xuan <william.xuanziyang@huawei.com>
> ---
>  net/can/bcm.c | 20 ++++++++++----------
>  1 file changed, 10 insertions(+), 10 deletions(-)

Both now queued up, thanks.

greg k-h
diff mbox series

Patch

diff --git a/net/can/bcm.c b/net/can/bcm.c
index 369326715b9c..bfb507223468 100644
--- a/net/can/bcm.c
+++ b/net/can/bcm.c
@@ -761,21 +761,21 @@  static struct bcm_op *bcm_find_op(struct list_head *ops,
 static void bcm_remove_op(struct bcm_op *op)
 {
 	if (op->tsklet.func) {
-		while (test_bit(TASKLET_STATE_SCHED, &op->tsklet.state) ||
-		       test_bit(TASKLET_STATE_RUN, &op->tsklet.state) ||
-		       hrtimer_active(&op->timer)) {
-			hrtimer_cancel(&op->timer);
+		do {
 			tasklet_kill(&op->tsklet);
-		}
+			hrtimer_cancel(&op->timer);
+		} while (test_bit(TASKLET_STATE_SCHED, &op->tsklet.state) ||
+			 test_bit(TASKLET_STATE_RUN, &op->tsklet.state) ||
+			 hrtimer_active(&op->timer));
 	}
 
 	if (op->thrtsklet.func) {
-		while (test_bit(TASKLET_STATE_SCHED, &op->thrtsklet.state) ||
-		       test_bit(TASKLET_STATE_RUN, &op->thrtsklet.state) ||
-		       hrtimer_active(&op->thrtimer)) {
-			hrtimer_cancel(&op->thrtimer);
+		do {
 			tasklet_kill(&op->thrtsklet);
-		}
+			hrtimer_cancel(&op->thrtimer);
+		} while (test_bit(TASKLET_STATE_SCHED, &op->thrtsklet.state) ||
+			 test_bit(TASKLET_STATE_RUN, &op->thrtsklet.state) ||
+			 hrtimer_active(&op->thrtimer));
 	}
 
 	if ((op->frames) && (op->frames != &op->sframe))