diff mbox series

[v6,3/4] riscv: dts: starfive: visionfive-v1: Setup ethernet phy

Message ID 20231220211743.2490518-4-cristian.ciocaltea@collabora.com (mailing list archive)
State Accepted
Delegated to: Conor Dooley
Headers show
Series Enable networking support for StarFive JH7100 SoC | expand

Checks

Context Check Description
conchuod/vmtest-fixes-PR fail merge-conflict

Commit Message

Cristian Ciocaltea Dec. 20, 2023, 9:17 p.m. UTC
The StarFive VisionFive V1 SBC uses a Motorcomm YT8521 PHY supporting
RGMII-ID, but requires manual adjustment of the RX internal delay to
work properly.

The default RX delay provided by the driver is 1.95 ns, which proves to
be too high. Applying a 50% reduction seems to mitigate the issue.

Also note this adjustment is not necessary on BeagleV Starlight SBC,
which uses a Microchip PHY.  Hence, there is no indication of a
misbehaviour on the GMAC side, but most likely the issue stems from
the Motorcomm PHY.

While at it, drop the redundant gpio include, which is already provided
by jh7100-common.dtsi.

Co-developed-by: Emil Renner Berthing <emil.renner.berthing@canonical.com>
Signed-off-by: Emil Renner Berthing <emil.renner.berthing@canonical.com>
Signed-off-by: Cristian Ciocaltea <cristian.ciocaltea@collabora.com>
Reviewed-by: Jacob Keller <jacob.e.keller@intel.com>
Reviewed-by: Andrew Lunn <andrew@lunn.ch>
---
 .../jh7100-starfive-visionfive-v1.dts         | 22 ++++++++++++++++++-
 1 file changed, 21 insertions(+), 1 deletion(-)
diff mbox series

Patch

diff --git a/arch/riscv/boot/dts/starfive/jh7100-starfive-visionfive-v1.dts b/arch/riscv/boot/dts/starfive/jh7100-starfive-visionfive-v1.dts
index e82af72f1aaf..692c696e1ab4 100644
--- a/arch/riscv/boot/dts/starfive/jh7100-starfive-visionfive-v1.dts
+++ b/arch/riscv/boot/dts/starfive/jh7100-starfive-visionfive-v1.dts
@@ -6,7 +6,6 @@ 
 
 /dts-v1/;
 #include "jh7100-common.dtsi"
-#include <dt-bindings/gpio/gpio.h>
 
 / {
 	model = "StarFive VisionFive V1";
@@ -18,3 +17,24 @@  gpio-restart {
 		priority = <224>;
 	};
 };
+
+&gmac {
+	phy-handle = <&phy>;
+};
+
+/*
+ * The board uses a Motorcomm YT8521 PHY supporting RGMII-ID, but requires
+ * manual adjustment of the RX internal delay to work properly.  The default
+ * RX delay provided by the driver (1.95ns) is too high, but applying a 50%
+ * reduction seems to mitigate the issue.
+ *
+ * It is worth noting the adjustment is not necessary on BeagleV Starlight SBC,
+ * which uses a Microchip PHY.  Hence, most likely the Motorcomm PHY is the one
+ * responsible for the misbehaviour, not the GMAC.
+ */
+&mdio {
+	phy: ethernet-phy@0 {
+		reg = <0>;
+		rx-internal-delay-ps = <900>;
+	};
+};